I keep thinking it’s time to write the epilogue, you know, with a final tweak or two to the Weber or ignition described, a break down of what it ended up costing and some video at 80 mph on a nice long back-road sweeper after the exhaust system is welded up. Well, it’s not that time yet. I keep having to revisit things I was taking for granted as done.
I guess the big lesson for me is that when rebuilding and installing the whole drive train, a bunch of the parts of which have never met before, there will always be one more thing to do before it’s done.
As usual- my teaser picture. I took this last week after I had just come down from my parts loft. As much as I am enjoying the challenge I would rather be getting on with the SS rebuild. Continue reading “101 1300 part 17: It ain’t over…”




As always, the teaser picture is actually the near final product. This carb looks pretty good but required $130 in new parts from my local Weber parts dealer. With the phenolic insulator block taking up about 6mm you can see the mounting nuts don’t fully engage the studs. Oh well, this is not a suspension component.
Here’s the new pipe mounted to the manifold with the asbestos heat shield bent out of the way. The oil pressure line is very close to the header with the heat shield in between. I plan on seeing if the pressure line can be bent or turned on the banjo bolt.
Here it is, fresh off the 00121 engine I am going to start rebuilding soon for the SS. It doesn’t look like much but the shaft spins nicely without having any side to side play. I am told these are pretty hard to find and expensive, so I will be careful.
As usual, the finished picture first. The red in the engine compartment came out good. Not great, just good. I think the level of finish in the engine compartment will match the rest of the car if I leave the valve cover alone.
Here it goes. A good quality hoist is key so you can lower it really slowly, allowing you to check clearances and guide it. Note the engine mount on the head.
Here I am at the first attempt, the easy out wasn’t so easy and even with a nut welded to the end it wouldn’t turn.